Well guys, i,m sure some of you would like to know how we got on today ??. There should be a new heading. "A bitter sweet day", firstly there are no pics, cos i forgot to bring home the camera, its in the boot of Worthers your thinking, Worthers must still be there . Correct. The day started well, Up in the air she went, filled up the diff, filled up the gearbox, and took some really nice pics. bled the brakes.. fine, down she came, my tick list was slowly going down, all nuts were tightened down, oil pressure pipe, temp sender, water drain, tick, tick, tick, carbs secured down, throttle cable sorted, i put ten litres of BP Ultimate in, no leaks, water and antifreeze in the rad, no leaks, all jubilee clips tightened, battery on, and secured, a final check of my tick list, gave Troy the thumbs up, turned the ignition key...........no lights, shit whats happened, after five minutes of checking, i,d then forget,when i,d put my new fusebox in, i hadnt connected the block connectors, very embarrassing. Tried again, she came to life, interior light worked, fan worked etc etc, Turned her over to get some pressure, plugs back in, WOW, she fired into life.... was set to 2500 revs and monitored for 20 mins, rev counter working, oil pressure gauge working, temp gauge slowly rising, no leaks, nothing, all going to well ????
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the revs were reduced, and thats when the problem arose there was petrol filling up in the forthport, it was fireing on three cylinders, not no.4, rev the car and it would be fine, try to idle and again, the port would fill up and idle on three, so in a nutshell,as of 9.38pm, thats were we are. Worthers in in Northampton awaiting tomorrow, Troy stripped the carb down, and it looks like there may be a crack, we wont know till tomorrow, so the bitter sweet bit is, it was going toooooooooo well, even the bits i,d done seemed to be working, he also checked the geometry on the car, even had it in gear with the rear wheels turning, gutted, thats all i can say.... lets see what tommorrow brings.
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Originally posted by ian parker View Postthe revs were reduced, and thats when the problem arose there was petrol filling up in the forthport, it was fireing on three cylinders, not no.4, rev the car and it would be fine, try to idle and again.
Welcome to IDF ownership !!!
those damn air jets.
All sounding promising though, how are your nerves though !!!!
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Originally posted by Kel View PostWelcome to IDF ownership !!!
those damn air jets.
All sounding promising though, how are your nerves though !!!!
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Well guys, heres the news ive certainly been waiting for had some time this afternoon and shot over to NMS, when i got there, Worthers was happily ticking over not too sure what the problem was, however its now been overcome. Troy did a couple of loaded runs on the rollers, it was great standing there watching her work, the rev counter, speedo, and the other three all showing positive readings, the one that did make my laugh was the fuel gauge, yesterday i put ten litres in, today, it wa bearly in the orange, but it was working, one slight concern Troy had was the downpipes closeness to the chassis rail, he,d wrapped it with some asbestos coated in a metal covering and it had done its job, no leaks, nothing, it appears a lot of hard work may well of paid off, gearbox sounded great as did the diff, some pics will follow shortly, i feel very happy as i,m writing this, get in there , now wheres those front seats
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